OPERATIONS

Transit to Site 1107

The 1930-nmi transit from Site 1106 to Site 1107 was accomplished in 7.8 days at an average speed of 10.2 kt. During the transit, preparations were made for deploying a reentry cone and casing. The reentry cone was assembled and moved onto the moonpool doors. The 16-in casing string was strapped, and a casing shoe was installed on the end of the 16-in shoe joint. The 16-in casing string was laid out on top of the riser hatch for immediate deployment upon arrival. The 103_4.gif (83 bytes)-in casing string was strapped and rabbeted in the riser hold, where it remained until time for deployment. The 16- and 103_4.gif (83 bytes)-in casing hangers and running tools were moved to the rig floor and fit tested. The 103_4.gif (83 bytes)-in cementing equipment, including the cementing head, kelly cock valve, and subsea release (SSR) plug, were also moved to the rig floor. The vessel arrived in the immediate area of the proposed site at 2012 hr on 22 May to be greeted by the Sonne. A positioning beacon was deployed at 2024 hr on 22 May, on the Global Positional System coordinates for the proposed site, officially establishing Site 1107.

Hole 1107A

The reentry cone was positioned in the center of the moonpool doors. The 48.8-m 16-in casing string was made up and latched into the reentry cone in ~5 hr. Making up the 16-in casing was slowed by excessive roll caused by two large cross swells affecting vessel stability. The jetting bottom-hole assembly (BHA) was made up of a 143_4.gif (83 bytes)-in bit, a bit sub, five 81_4.gif (82 bytes)-in drill collars, a 16-in Dril-Quip CADA casing running tool, two 81_4.gif (82 bytes)-in drill collars, a tapered drill collar, and two stands of 51_2.gif (82 bytes)-in drill pipe. The jetting BHA was latched into the 16-in casing hanger, and the reentry cone/16-in casing string assembly was lowered to the seafloor. The camera was also deployed to observe the position of the reentry cone after jetting in and to observe release of the 16-in casing running tool.

No pilot hole or jet test was performed before jetting in the 16-in casing at Hole 1107A. The location of Hole 1107A was positioned between Holes 757B and 757C, which are 200 m apart and were drilled during Leg 121. The length of 16-in casing to be jetted in at Hole 1107A was determined based on advanced hydraulic piston corer data from Leg 121. Also, the seafloor depth established during Leg 121 was used for starting the jetting in process for Hole 1107A. However, the official water depth of 1659 mbrf was determined by tagging the seafloor with the end of the 16-in casing, which was determined to occur at the first noticeable pressure change while initiating the jetting in process.

Jetting in of the 16-in casing began at 1455 hr on 23 May, establishing Hole 1107A. Jetting in the 48.8-m of 16-in casing was accomplished in 2 hr, 21 min. The camera was used to determine that the reentry cone mud mat was positioned properly, sitting on the seafloor. The 16-in casing running tool was unlatched and retrieved with no difficulties. During the trip out of the hole, two Woods Hole Oceanographic Institution (WHOI) OBSs were deployed and surveyed relative to Hole 1107A as part of a SWD experiment. A ship-to-ship transfer from the Sonne of blasting caps and a ranging transducer was also completed.

Once back on deck, the 16-in casing running tool was removed and an additional 81_4.gif (82 bytes)-in drill collar was added to make up the 143_4.gif (83 bytes)-in drilling BHA. The 143_4.gif (83 bytes)-in drilling BHA was tripped to the seafloor, and the reentry cone reentered at 0543 hr on 24 May. The hole was drilled ahead to a depth of 2081 mbrf (422 mbsf) with mud sweeps as follows: 1 × 25 bbl at 1810.4 mbrf (151.4 mbsf); 1 × 25 bbl at 1897 mbrf (238.1 mbsf); and 1 × 30 bbl at 2081 mbrf (422 mbsf). As soon as the BHA was below the seafloor the Lamont-Doherty Earth Observatory (LDEO) sensor sub, part of the SWD experiment, was installed. The sediment portion of the hole drilled slower than anticipated with rates of penetration (ROPs) as low as 4 m/hr. However, the hole remained stable with little, if any, fill at connections.

Contact with basement was made at a depth of ~2030 mbrf (371 mbsf). Unlike the sediments, the basement initially drilled faster than anticipated with ROPs as high as 8 m/hr. The original drilling plan called for ending the 143_4.gif (83 bytes)-in hole at a depth of 2069 mbrf (410 mbsf). However, firm basement was not encountered until a depth of 2063 mbrf (404 mbsf) had been reached. Therefore, the decision was made to continue drilling ahead until at least one full joint of casing could be positioned below the hard basement contact.

A wiper trip was made to a depth of 1692 mbrf (33 mbsf, inside the 16-in casing) with a maximum overpull of 10,000 lb. The LDEO sensor sub was removed during the wiper trip in preparation of running the 103_4.gif (83 bytes)-in casing string. The hole was allowed to stabilize for 1 hr, and then the bit was slowly tripped back to bottom. A moderate drag of 20,000 lb was observed near the sediment/basement contact at a depth of 2035 mbrf (376 mbsf). The top drive was picked up, and the hole was washed and reamed through the sediment/basement contact area. Once the bit was back on bottom, the hole was swept with a 30-bbl mud pill and then displaced with 346 bbl of sepiolite mud. The bit was then retrieved in preparation for deploying the 103_4.gif (83 bytes)-in casing string.

A 413.2-m-long string of 103_4.gif (83 bytes)-in casing, including the remaining 23 joints of 103_4.gif (83 bytes)-in standard coupling casing on board, was made up in ~5 hr. A cementing BHA consisting of a 103_4.gif (83 bytes)-in SSR cementing plug, a 103_4.gif (83 bytes)-in Dril-Quip casing running tool, five 81_4.gif (82 bytes)-in drill collars, a tapered drill collar, and two stands of 51_2.gif (82 bytes)-in drill pipe was made up and latched into the 103_4.gif (83 bytes)-in casing string. The 103_4.gif (83 bytes)-in casing string was then tripped to the seafloor, and Hole 1107A was reentered at 1515 hr 26 May.

The casing was run to depth when the top drive, kelly cock valve (used to prevent cement from flowing up into the top drive), and cementing head were picked up. The drill string was then spaced out to land the 103_4.gif (83 bytes)-in casing hanger inside the 16-in casing hanger. After landing the 103_4.gif (83 bytes)-in casing hanger, latch-in was confirmed with a 10,000-lb overpull. From reentry to latch-in, confirmation took ~2 hr, with no difficulties encountered.

The 103_4.gif (83 bytes)-in casing was successfully cemented in place with 238 sacks (48.8 bbl) of silica flour blended 15.8 lb/gal cement. While displacing the cement, the pipe wiper plug dart was dropped on top of the cement slug and chased with a 10-bbl freshwater spacer and then seawater. Landing of the pipe wiper plug dart in the SSR plug was confirmed with an increase in drill-string pressure. While we pressured up the drill string to release the SSR plug, the cementing hose burst near the connection with the cementing head at ~2000 psi, requiring the pump to be shut down immediately. Fortunately, at that time the cement slug was contained within the casing below the SSR plug (with the latched in dart) and the casing shoe.

Using a tugger, the driller was raised in the derrick to the heaving cementing head, where he broke off the ruptured cementing hose and replaced it with a blanking plug. Once this was accomplished, the driller also had to manually open the kelly cock valve above the cementing head, so a circulation path through the top drive could be established. After the driller was safely back on the rig floor, the pump was re-engaged and the drill string pressured up immediately, indicating that the SSR plug and dart had remained in place. The drill-string pressure was increased to ~2800 psi when the SSR plug released and was pumped to the casing shoe. Upon landing of the SSR plug in the casing shoe, a solid 600-psi pressure was held for a few minutes. The stand pipe bleed-off valve was then opened, and no flow back was observed, indicating that the casing shoe valve was holding. The only task remaining was to release the casing running tool. It required ~45 min of working the 103_4.gif (83 bytes)-in casing running tool before it finally was released and the drill string could be retrieved.

The original drilling plan called for coring Hole 1107A to a depth of ~200 into basement. However, with the lost time in port rebuilding the lower guide horn, there was not time to core at all, let alone hope to reach a depth of 200 m into basement. The decision was made to deploy a 97_8.gif (82 bytes)-in tricone drill bit and drill as deep into basement as the remaining operational time allowed in the hope of leaving an acceptable hole for the future installation of an ION seismometer. A 97_8.gif (82 bytes)-in drilling BHA was made up consisting of a 97_8.gif (82 bytes)-in tricone bit, a bit sub, eight 81_4.gif (82 bytes)-in drill collars, a tapered drill collar, and two stands of 51_2.gif (82 bytes)-in drill pipe. The 97_8.gif (82 bytes)-in drilling BHA was tripped to the seafloor, and Hole 1107A was reentered at 0738 hr 27 May.

The 103_4.gif (83 bytes)-in casing shoe was drilled out in 43 min. The rathole below the 103_4.gif (83 bytes)-in casing shoe was cleaned out, and then a 97_8.gif (82 bytes)-in-diameter hole was drilled into basement to a total depth (TD) of 2152.8 mbrf (493.8 mbsf, 122.8 m into basement, 79.4 m below the 103_4.gif (83 bytes)-in casing shoe, Fig. F6). A schematic drawing of the NERO borehole installation is shown in Figure F6. A single 25-bbl mud sweep was pumped at 2107.4 mbrf (448.4 mbsf). At TD the hole was flushed clean and a 30-bbl mud sweep was circulated. With the hole cleaned up as much as possible, and with operations time expiring, the bit was retrieved. The bit cleared the rotary table at 0640 hr 28 May, ending Hole 1107A. During the trip out of the hole, the two WHOI OBSs were recovered. The vessel was secured for sea and the transit to Darwin, Australia, began at 0730 hr on 28 May.

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